mirror of
https://git.kernel.org/pub/scm/linux/kernel/git/next/linux-next.git
synced 2025-01-13 09:20:17 +00:00
a6fe5e52d5
pm_runtime_get_sync() and pm_runtime_put_autosuspend() return 0 on success, 1 if the device's runtime PM status was already requested status or error code on failure. So a positive return value doesn't indicate an error condition. However, any non-zero return values from buffer preenable and postdisable callbacks are recognized as an error and this driver reuses the return value from pm_runtime_get_sync() and pm_runtime_put_autosuspend() in these callbacks. This change fixes the false error detections. Cc: Daniel Baluta <daniel.baluta@gmail.com> Signed-off-by: Akinobu Mita <akinobu.mita@gmail.com> Cc: <Stable@vger.kernel.org> Signed-off-by: Jonathan Cameron <Jonathan.Cameron@huawei.com>